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Overview

Statistic
Value
Propellant Weight~ 42.4 lb *
Impulse39307 Ns
Max Pressure739 psi
ClassificationO12655
Delivered ISP208 s
Grains

OW-152 #17-#24

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ENG File:  P2.eng

Discussion

Observations

•Erosive burning spike was observed in thrust curve, then progresses with normal BATES thrust profile until nozzle failed
•Nozzle cracked at phenolic interface
•Casting tube was likely ejected at +3 seconds around the same time the nozzle cracked, corresponding to the burnout of the aft grain
•Liner surrounding aft grain was ejected at +6 seconds
•Leak path at nozzle crack led to significant loss of pressure and thrust

What caused this?

•Increased Al combustion in high L/D motor raised temperature and interacted with other compounds to enter an uncharacterized combustion regime
•Nonlinearity in burn rate law (r = aP^n) unrelated to Al combustion
•Burning on outside of grains (inside of casting tubes)

Reconstruction of Events

•T-0: The igniter actually works and motor ignites
•T+.5: Erosive burning spike settles down, but motor is now burning at a much higher pressure than expected due to higher Al combustion effect on burn rate law
•T+.5 - 2.9: Thrust curve follows typical BATES profile
•T+2.9: Aft grain burns out, casting tube is ejected
•T+2.9: Interaction with casting tube event along with elevated thermal and mechanical stresses causes nozzle failure
•T+2.9-6.2: Motor continues to burn at lower pressure/thrust due to fewer grains, leakage at nozzle break
•T+6.2: Second grain from aft end burns out, unprotected liner at aft end is ejected due to high velocity gas passing over it
•T+7.8: Motor shuts down

Where do we go now?

•Option 1: Build the same motor again for SAC and reconsider the vehicle’s structure to handle higher loads
•Option 2: Redesign the motor for combustion in the “aggressive” regime, static test it, and then rebuild it for SAC
•Option 3: Redesign the motor for the “aggressive” regime, but don’t static test it before SAC
•Option 4: Descope to 4G motor

How much additional money would the team need to spend to complete each option?

•Option 1: $690 (not including structural redesign)
•Option 2: $1,137
•Option 3: $690

The burn began nominally and continued for approximately three seconds, however, at the three second mark, the case ruptured in a large fireball that engulfed the test stand. The failure led to a rapid loss of thrust and damaged the test stand and several sensors in the surrounding area.

Upon inspection of the motor after the anomaly, it was almost immediately clear what the source of failure was. The motor split at approximately the same location at which the liner was spliced.

Failure theory:

During liner splicing in the past, Gorilla Glue was applied to the middle grain that contained the splice joint. The two halves of the liner were slid on opposite ends of the grain and pushed together, meeting at the halfway mark in the grain. RTV was applied to the seam and a piece of clear packing tape was applied at the seam to facilitate insertion of the grain assembly into the liner. There was typically a bulge of RTV that was covered by tape at the splice point, as shown below.

In preparation for this static fire, the liner halves were pushed together on the middle grain until they were two inches apart, and then the RTV was applied and the tubes pushed together. This may have caused a problem because the resulting mixture of Gorilla Glue and RTV may have either not cured, or cured with dubious thermal properties that were compromised when hot gases seeped to the middle grain during the burn. Further, the majority of the RTV on the seam was scraped off the splice joint because it was thought that there was enough RTV already in the seam to form an adequate seal. This proved not to be the case, however. From the post-test footage, one can see the case discolor and bulge at the splice point moments before the failure, showing that the liner splice likely failed instantaneously upon ignition and that the case was exposed to combustion gases for the entire three seconds leading up to failure. This is evident from the cooled aluminum drips on the test stand base that indicated that much of the material at the splice point was melting before the case ruptured.

Splice for failed static fire, OW-152-8G#2

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Splice for successful static fire, OW-152-8G #1

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Resolution:

In the future, the team will research liner splicing methods more thoroughly before attempting another liner splice in the fall. We are reaching out to other schools that have attempted liner splices before to gain more insight on the process can be performed more reliably in the future.

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